Status Report

ISS MER Status 1 June 2001 (from Felicity Vol. 62)

By SpaceRef Editor
June 1, 2001
Filed under , ,

Excerpt from: 1 June 2001: Felicity Vol. 062 (2 MB Acrobat)




Problem Title
Problem Description Current Status
C& C MDM Failures Multiple C& C MDM failures. All three C& C MDMs have functional MSDs loaded for 7A. C& C 3 – PRI, C& C 2 –
B/ U, C& C 1 – STBY. Approx. 151/ 14: 10 GMT (9: 10AM Thurs. 5/ 31) there was a
“MSD Inaccessible” flag set on C& C 3.
4B BGA High Torque BGA 4B showed motor torque values reached an
average of 270 in- lbs during a four minute
interval while performing nominal rotation for
power- charging. During this interval, a maximum
torque of 320 in- lbs was recorded.
4B will stay in directed position mode. Team is investigating flying a replacement
BMRRM on a future flight (7A. 1).
BGA 2B Current Spikes Higher than expected BGA motor drive currents
(up to 0.6A) during rotation.
On- orbit data indicates that baseline 2B BGA motor currents are not increasing
over time, but current spikes are increasing in magnitude and frequency. An
open loop test has been conducted and the results are under analysis.
N1- 3B- A RPC 16 Trip RPC feeding Node Smoke detector tripped
unexpectedly after performing maintenance on
the adjacent HEPA filter
Power on of smoke detector for 2 sec. to detect a short was done with no short
indicated. Additional T/ S planned.
Ku- Band Gimbal
Temperatures
Ku- Band gimbal temperatures repeatedly drop
below certification limits.
Team is investigating the feasibility of adding thermal blankets or adhesive
heaters to the Cross- Elevation gimbal on a future EVA.
MCA Electrometer Op
PBIT
MCA unexpectedly shuts down Intermittent shut- downs continue. Plan to R& R unit before 7A.
MCOR Overtemp MCOR shutdown due to overtemp The MCOR was manually shut down during its early operation when it exceeded
40 degc. The MCOR ART is evaluating the 40 degc operational limit, and will
propose a software change to increase this limit to possibly 47 degc.
Possible Lab Window Contamination Lab window cover was left open during Soyuz docking resulting in potential contamination from the Soyuz RCS jets. Procedure is in place to establish rules for closure in order to minimize accummulated contaminants for all flights. A special rule has been drafted for the 7A mission.
ECOMM Connector FOD During ECOMM antenna removal from the Node
1 Stbd port (EVA 2), a wing nut (approx. 2.5
inches) came off of one of the connectors. This
connector was attached to the hatch ECOMM
plate. FOD suspected from this wing nut is a
total of three items.
Crew will monitor CBM operations during 7A. The hatch will also be moved to the
Test position during 7A before the EVA to determine if any hatch repairs must be
made before Airlock berthing operaqtions.
Redundant String ACU (Arm Computer Unit) Brake Voltage Errors During Brake Release Received Alarms: “R3B – SSRMS ACU DPRT Brk Switch Fail”, “R3B – SSRMS ACU DPRT Brk Voltage Fail”, “R3B – SSRMS Brk Voltage Err”. The alarms occurred during the extended jont range test, while in redundant string. The SSRMS safed automatically. The failure has not recurred and troubleshooting has failed to reproduce the problem. Anomaly resolution team investigation is on- going with no clear cause of the problem being identified.
Shoulder Pitch JEU Anomally Received R3C SSRMS SP JEU Transmit and Receive Errors while SSRMS operational on redundant string, but not being used. JEU was rebooted, and failure was reanunciated The failure has persisted since the original occurrence. Troubleshooting is ongoing and has narrowed the list of possible failures to the Arm Control Unit or the Shoulder Pitch joint. Diagnostic software is being developed to characterize the events that led to the failure.
Unable to evacuate CDRA CO2 bed After sucessful R& R of the CDRA Airsave pump,
the CDRA was unable to pump down the
AD/ DES 1 bed.
Has operated in single- bed mode successfully. Replacement check valve is available on- orbit, but replacement plan is still being established (valve is not designed to be an ORU).
CMG Loss of Attitude Control During operations to swap from US C& C2 to
C& C3, TsUP commanded communication to be
broken on the busses between the SMCC and
the US C& C. Because the SMCC had no
communication with the US C& C, the RS then
started a timer (5 minute default) after which time
they unconditionally took control. This led to a 3
minute force fight, after which the US CMGs
reached saturation, and the US GN& C declared
loss of attitude control
After discussions between US and Russian engineers the situation is
understood. The area of investigation focuses on why TsUP thought it
necessary to inhibit higher bus communication and why autohandover was not
inhibited since this is a planned response to the communication interuption.
CMG 2 Survival Heater Activation CMG 2 spin bearing temperatures began to rise
unexpectedly. The termperatures went from
about 27 deg C to about 43 deg C within 6 hours.
This temperature increase was attributed to the
CMG survival heater coming on, so the RPC to
the survival heater was opened, and the
temperatures immediately began to decrease.
Analysis of data indicates that the survival heater performed nominally for the
given thermal environment (powered on due to decreased temp from being in
shade). The behavior also matched thermal predict for this case. Predicts also
show that the heater would have cycled off had the RPC not been opened.
ESP Survival Heaters Off since 6A Power was removed from the ESP- 1 primary and
secondary heaters during the 6A mission and
they were left off until it was discovered
approximately 30 days later. ESP- 1 houses a
spare PFCS and a spare DSCU.
A procedural error. Investigation into what caused it and how to keep it from
happening again is underway.
SSRMS Anomalies Check- out operations on the redundant string
have indicated a problem with either the ACU,
the JEU (for the shoulder pitch joint), or the
connections in between.
An ART is in the process of identifying further trouble- shooting tests. In parallel,
wrok is underway to prepare for the potential requirement to change- out either of
the ORUs on a future flight, ir required.
BGA High Current BGA 4B has indicated high current during
rotation and movement.
The ART is working to determine the root cause and potential action. Testing
has been conducted on both 4B and 2B to further characterize system
performance. Power generation and loads are also being analyze to ensure
ade quate margins for assembly missions and free- flight.

SpaceRef staff editor.